Six Sigma Training – Is it worth the
investment? Using the new model the trainee Black Belt was able to determine the optimum process settings, which confirmed that the process standard deviation could be reduced by 40% resulting in a 20% unit cost reduction and an 80% lead time reduction. The resultant savings were in excess of €125,000. Fig 1. Printed patterns from the screen manufacturing process show the before and after surface area variation.
The second project successfully reduced the defect level of specific components being shipped to one of their European customers from 611 ppm to approximately 45 ppm. This project proved more difficult as most of the defects were due to ‘special cause’ variation but using tools such as process mapping, failure mode and effects analysis and mistake proofing, ppm reduction was achieved and more importantly sustained, generating annual savings in excess of €114,000. Our second company is Molex, based in southwest Ireland. Molex is the world's second-largest manufacturer of electronic, electrical and fiber optic interconnection products and systems. Molex also manufacture a variety of switches and application tooling. Molex has product development centers, manufacturing facilities and sales offices on six continents. The Irish plant were challenged by a 28,000 ppm internal reject level on a new product line. Initial investigations identified that resistance failures made up 70% of the problem. The second discovery was that the 28,000 ppm was only achieved by retesting ‘failed’ units (44,000 ppm from the first test). Therefore the focus was immediately drawn to the resistance test equipment. Using team tools such as process mapping, cause and effect matrices and process failure mode and effects analysis (FMEA), the source of many of the false rejects were identified. Two immediate changes were implemented bringing the ppm level down to 11,500 ppm. However, a measurement system study continued to puzzle the team as they struggled to get the three resistance testers to agree exactly in repeated tests. Following some research into the linearity of resistance measurement devices at low resistance levels (below 1 ohm), a breakthrough discovery was made. While resistance measurement was indeed linear above 1 ohm, when measurements fell below 1 ohm there was a non-linear relationship. The problem was solved by developing resistance standards of 0.33 ohms and 0.5 ohms to allow for more accurate calibration at lower resistance levels. By eliminating this linearity problem and a bias problem between the three testers, the team got all three to accurately repeat in a guage R&R study. The result was a drop to 4000 ppm, with all three testers giving comparable results. The trainee Black Belt’s diligence and perseverance resulted in an 85% reduction in reject level and savings of over €75,000 p.a. Fig 2. Project performance showing dramatic fall in PPM
Collectively these 3 projects delivered cost savings in excess of €300,000. So what about return on investment? Well, how many training programmes do you know can deliver a hundred-fold return on initial investment within the year? If you keep in mind that trained Black Belts should be capable of completing at least two major projects a year, then the return on investment should be more like 300-500%, even with an 80% project success rate. Now that’s what I call a real measure of training effectiveness!
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